Sunday, March 25, 2018

Generac

Servicing a residential back generator. Natural Gas fueled. So happy the front housing cover comes off, made the oil change much easier. Using a pump to such l out the oil certainly speeds things along as well.




Generac transfer switch doesn't have the control to set the exercise time, unlike some other transfer switches, but I was able to set it through the control panel on the generator itself .
                     

Many home generator units look alike, but have little differences in control panels, housings,  and transfer switches. My job entails learning the differences and how to service and test whichever ones I come across.

Engine swap update

Donor engine finally in destination engine bay, bolted down and connected to tranny. New parts: pilot bearing, throw out bearing, water pump,  several gaskets, rebuilt injection pump, a couple injectors, return line kit, and probably a few more to come. 


What a project, taking a long time mainly because I only get one day a week to work on it. Two engine pulls, and one installation in progress.

Monday, February 12, 2018

Engine swap project update

The engine swap is going well I'm glad to say. Since this is the donor truck, and cab will be removed, I decided to go ahead and remove the grill, and core support to make engine access much easier. All that's left to pull the engine is to pull the bellhousing bolts and engine mounting bolts.


Deflected deflector and reaming.

Last week I started a blog on an inline 10 cylinder injection pump, here is the continuation. 

Once I finished teardown, I found damage in the a pluger bore. One of the player assembly reflectors had moved and the higher pressure cut through the narrow part of the bore wall into the next bore. 


Here's the plunger assembly with the deflected deflector. It's the part with the small holes, it should be up against the body. 



Another project I had was to install and ream new bushings in an injection pump housing. I got a picture of the reamer during the process. Lots of tapping fluid and some patience yielded a good result.



Monday, February 5, 2018

Injection pump teardown

 After being sick for almost a whole week, a couple weeks ago I started doing some work for the fuel shop part of the business, a change in direction, and new learning experience, from vehicle and generator service.

Last week I started tearing down a unique 10 cylinder inline injection pump. The teardown is going well, it's slow, but I'm learning the steps involved.

Torch pictured was to hear up body to get a plug out.

Important to keep sections coming off pump during tearing together so they will go back together in same position, and not get mixed up.


Pulling freeze plugs was tedious, but gives access to next phase of teardown. My day ended after this step.

To be continued next week...

Monday, January 15, 2018

Engine swap

Engine swap project started. Started by pulling accessories off engine. 



 Continued


Inside top of DB2 injection pump. Pulled pump to check it out, showing evidence of presence of water.

Wear showing in advance bore.
                        




 Corresponding wear on advance plunger. Pump to be rebuilt, then installed on donor engine when ready.



Monday, August 21, 2017

VW Intake blockage

One of my projects last week. Owner of 03 VW TDI complained of  lack of performance, and check engine light on. The egr, and egr cooler had previously been cleaned, and the MAF sensor replaced. The customer mentioned the intake had also been cleaned out in attempt to fix the issue. The engine ran better with MAF sensor unplugged(it reverts to default setting in computer I believe), but wouldn't rev or get up to speed anywhere close to how it should've. We decided to check the intake runners, and intake ports in the head, to check for coking blockage.


Intake manifold behind the egr. It looks wet, but is dry.

Ready for intake removal


Soaked intake with solvent during lunch.


This coking was mostly in the elbow between the intake plenum and the runner the the egr bolts to. It was missed by whomever had cleaned the intake previously. There was almost 3/4 of a cup of material blocking air flow. 

After re-assembly the car was test driven, and performed as it should, no hesitation to reving, and drove well.

I learned to be thorough when cleaning parts, as the blockage in the elbow of the intake could easily be missed(as it was by previous technician who performed the procedure), and the problem would not be fixed.

  Week 7: 40hrs
Total: 280hrs